I've got a couple days back on the road with the clutch pivot fix. In the thrash to get stuff back together I didn't really snap as many pics or document the added little work done along the way so I'll just describe some of the work and let your imaginations run wild.
Oil change was done while up on blocks. Simple but satisfying.
The passenger side engine bracket provided from Kpower had clearance issues with the block in one spot. I found out about this after I had already dropped my engine into the bay but never checked to see if it affected me. With the header out I pulled the bracket and confirmed we have contact so a grinder sorted the protruding block material. Sorted.
When pulling just the trans, it needs to slide rearward obviously but the stock trans tunnel bracket is kinda in the way near the bolt locations. After wrestling it out using some force with a pry bar I decided to make install easier trimming a bit more material on both sides. With a little flapper wheel work it was good to go.
Since I have been using the shortened stock shifter I no longer have to use a trimmed shifter plate that the console would normally be screwed to. The Kpower kit requires you to cut off a bracket for their shifter plate, but this makes the console a bit wobbly and less secure. I think it also made NVH more noticable and transferred to the dash area. Anyway, I replaced the cut piece with a stock one and now the console is solid again. I didn't think it was that big of a deal but after having it back I wish I would have just made a bracket or modded the original one from the beginning to fit. Here's a pic of one that isn't cut. The two small holes on the left are what was cut off.

The front of the timing cover was covered in oil cosmoline again so I started wiping everything down looking for the leak point. Apparently the crank sensor bolt took a vacation and didn't come back. Luckily the oil seal held it in the cover but still allowed some oil out. I don't think it was causing any issues running but another bolt thrown in fixed the issue.
My passenger seat lever has been buzzing at idle and low RPM for quite a while. It's maddening. I would go a day or two without it being a problem but it seems most prevalent when it's cold outside. Anyway, after getting the car back together I decided to pull the seat and figure out a solution. I thought I could just dampen the buzz with felt where there's contact but because of the lever setup this wasn't possible. I ran to the parts store and found a carb spring kit in hopes I could rig somthing up. BINGO. I added one spring to keep tension on part of the lever that's hidden behind a cover at the top of the lever. No more noise and you can't see the fix at all from any position. Done.
Next was a dash buzz around the glove box. I replaced the glove box with a newer/used one in better shape but the sound persisted. While the seat was out I found that the lower section that the glovebox clips into has a metal backing bracket thing. It has just enough gap between the bracket and the lower portion of the dash to create the infamous buzz in low RPM mainly sitting idle at a stop light. So I wedged some felt between the two and I'm happy to say it's gone. Next!
The very front lip of the dash where it meets the windshield base has some foam that kinda takes up the difference when in place. Unfortunately maybe a combo of me removing the dash a few times, the vibes from the k24, or just age has allowed the dash in that spot to buzz. If I lightly place my hand on that spot the buzz goes away. So I took some foam used for HVAC gaps and slid it in where the stock stuff is adding just a little more in stack height. This gave it just enough pressure to hold the dash steady.
Driver side dash speaker plastic will buzz sometimes where it meets the A pillar trim. Not all the time but enough to be annoying when it does. I added some felt in some places before but it never seemed to fix the issue. Realizing that foam I used on the dash might be able to apply the needed pressure I cut a few small pieces to help take up the gaps and keep it solid. Heck yeah, we have an almost silent interior when at idle now!
All in all with the trans back in, and almost every annoying noise I could track down eradicated, I'm pretty happy with the car again. It's the little things that make it a better daily and these made a huge impact. I received the new jumper board to install the fuel pump relay, so that will get installed soon at some point. I'm not in a hurry to get under the dash again but it would be nice to just have it done. That's enough words for now. Ciao.